The tremendous racket produced by the hydrantlike force of water striking deck plates and other structures in the engine room made it almost impossible to talk. I put my mouth next to Don Fear’s ear and shouted, “Good Lord, Don, how long has it been this bad?”
Fears looked serious and shouted into my ear in turn. “This is why I called you, Captain. The leak we had before was getting slowly worse and I was thinking of calling you anyway, then suddenly she broke loose.”
“What is the trouble?” I yelled.
Don shook his head. “Don’t know for sure, sir. Curt and his people have been right on it, though. Maybe we’ll have an answer pretty soon.”
“You can’t handle this with the drain pump, Don,” I shouted, enunciating slowly and carefully above the din. “We can’t let these bilges get too full!”
Don nodded understandingly. “We have the drain pump on the line already, Captain, but I think you’re right. The pump won’t be able to keep up with this flood!”
Quite apart from the ultimate safety of the ship herself, if this huge leak could not be stopped, there was a lot of electrical equipment and other delicate machinery in the engine room which would be damaged if the water level rose too high.
“Don,” I said, “we’ll have to stop the starboard shaft. That will help some. At least it will let Curt get closer to the problem. I don’t like him working around the shaft like that while it’s turning.”
Don nodded, shouting in my ear. “Maybe we could come to a shallower depth, too, Captain. That would reduce the pressure and cut down the leak some.”
I assented. It took but a second to dash up the ladder to the upper level, find a telephone, and call the Officer of the Deck. In a moment, the starboard propeller shaft began to slow down, and at the same time the ship angled gently upward. In deference to the amount of water already in the bilges, which would all be concentrated in the after end if too steep an angle were assumed, I had told the Officer of the Deck to bring her up handsomely—that is, slowly and steadily, with good control.
As the outside water pressure was reduced, the leak correspondingly decreased. Shellman cast me a grateful look. I beckoned to him. “Curt,” I said, “we are locking the shaft so that it can’t turn. This will let you get closer to it, at least.”
Shellman was mopping his face with a rag. “Thanks, Captain. I was about to ask if we might do that. I’m afraid to put somebody outboard of the propeller shaft because there’s not much clearance between it and the skin of the ship.”
He did not need to say more. There was perhaps a foot-and-a-half clearance between the propeller shaft and the curve of Triton’s pressure hull or skin. As I watched the propeller shaft come to a complete stop, there came into view a great bolted coupling by which two sections of the shaft had been joined together. The huge coupling had been rotating previously in a sort of a blur, its machined edges a lethal hazard while the shaft was turning.
With the shaft at a complete halt, Curt and Chief Engine-man Fred Rotgers climbed on top, braving the reduced spray of water, while “Rabbit” Hathaway, a compactly built Engine-man, squirmed under the shaft and into the confined space.
Several minutes later we had the answer. The spit of anger in Rotgers’ voice as he reported the basic cause of the problem was not all due to the salt-water bath he had just experienced. “The _____ nuts on the far side of the gland are so loose you can turn them by hand,” he spluttered.
“How about the locking washers, Chief?” asked Shellman.
“I sure didn’t see any. That’s why they loosened up!” Rotgers glared as he spoke. It was evident that whoever had installed these bolts would have fared badly had the powerful Rotgers been able to get his hands on him at that moment.
“There are locking wires on the inboard side of the gland,” reported Shellman, after a brief inspection.
Further investigation showed that loose bolts were not the end of the trouble. The propeller shaft water seal had been improperly installed, that is, not made tight, either because of the difficulty in reaching some of the bolts or through lack of locking devices. Under the vibration and stress of continual high speed, complication had followed upon complication. Looseness of the bolts on the outboard side had permitted the packing gland to become partially cocked on its seat, and now, tighten the bolts as we would, it remained jammed in a cocked position and could not be straightened. We heaved on the nuts with the biggest wrenches aboard, to the point where Curt feared further pressure might distort or damage the parts even more, but there was no stemming the leak.
Not sure, in fact, whether or not some improvement might have been made, we eased Triton down again into the depths, and the resulting effect, with the greater pressure outside, was striking, to say the least.
We had obviously not solved the problem. The next step was to put an emergency clamp around the leak, utilizing three damage-control clamps which had been designed for small patches, not for anything as massive as this. Down we went for a test again, but the pressure of the water was so strong that it simply pushed the clamps apart.
Midnight had long given way to morning as Curt Shellman, Fred Rotgers, Clarence Hathaway, and others struggled with the leak in the confined space. The watch had changed at midnight and again at four o’clock, but Shellman, Rotgers, and company stayed on the job. Two solutions were decided on: first, we would try to reinforce the three damage-control clamps which had failed; second, we would design an entirely new clamp, sacrificing for the purpose a section of molding from the wardroom passageway, which happened to be made of corrosion-resisting steel and was, by good fortune, of sufficient size for our use.
By breakfast time the first try was in place, damage-control clamps with backing plate for reinforcement. It had been a long, back-breaking job, performed in tight quarters under the most unfavorable conditions, with water squirting in under pressure the whole time the men worked. When we unlocked the propeller shaft for a full-fledged test, Curt Shellman’s naturally haggard face assumed an even more worried expression, the deep circles under his eyes standing out almost as though the difficulty had caused him physical suffering. But all went well; the leak did not increase beyond manageable size, the drain pump was able to take care of the water leakage without difficulty, and Shellman permitted a half-smile to wrinkle the deep bags under his eyes. At noon, Fears reported that the modified clamp would hold, for the time at least, and that our newly manufactured one would be held in reserve.
Entry from the Log dated 12 March, 1960:
0020 Our fathometer is out of commission again. This is bad news. It has been giving us trouble off and on for the past several days. Each time, however, we have brought it back into operation. This time, as our electronics technicians and sonarmen check it over, they actually record the gradually decreasing installation resistance in the head. It appears to be flooded.
Ever since the initial difficulty with the fathometer, “Whitey” Rubb and Dick Harris had been giving me daily reports as to its condition, and I was well aware of their increasing fears as to its performance. All the instruction books we had on board for the fathometer had been pored over, and in anticipation, we had checked over the stock of electronic spares on board the ship, the back-up for all the complicated electronic-control equipment with which Triton was fitted. All spare parts which could conceivably be used in the fathometer—tubes, resistors, crystals, power amplifiers—all, no matter what type of equipment they were originally designed for, had been located, so that we could substitute as necessary.
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